艾里逊变速箱油:隧道类英语比较厉害的高手帮翻译下。

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2.1. Collapse zone (Ch: 36+617–36+610)
Collapse took place in an oversaturated fault gouge zone lying behind the face and dipping steeply into
the tunnel. The occurrence and the large extent of the collapse zone resulted from the failure to locate the
fault zone and by delaying installation of necessary support elements during the previous round of excavation cycles (between Ch: 36 + 625 and 36 + 617). Absence of rock bolting in the initial support system, the highly stressed nature of the rock mass and softening or loosening of the clayey material in the
fault gouge contributed to the occurrence of collapse.Initially, water started flowing through the left sidewall
of the top heading as dictated by the natural hydraulic gradient, and gradually extending the eroded zone towards the floor. Eventually, the tunnel was filled with 92 m3 of collapse debris (Fig. 6). The flow rate recorded in this segment reached 3 l/s.
To prevent the spread of the collapse, this pile of debris supporting the remaining part of the excavation face was quickly dammed and stabilized by external materials. Following this, a total of 28 m3 of shotcrete was applied to the collapsed area to create a 20-cmthick rigid layer. Subsequently, additional stabilization measures and support installation between Ch:36 + 617 and 36 + 610 were carried out in the following sequence: (a) a total of 33 forepoling pipes (length:6 m, /: 1.5 in.) were driven along the roof section of the collapse face to form a rigid canopy; (b) wire mesh (/: 131–131) was fitted on to the initial shotcrete layer with the help of T-shaped drive-in bolts; (c) an additional layer of 16-cm-thick shotcrete (22 m3) were formed; and (d) a total of 12 rock bolts (length: 8 m, /:28 mm, ultimate load: 25 t) and 27 NPI steel ribs were installed.
Following the prevention of collapse zone enlargement, 44 m3 (BS 20) of concrete and 80 m3 of shotcrete were used to restore the tunnel section in the collapse area. Then consolidation grouting using
various cement mixture ratios (cement/water ratio:1/1, 7/5 and 7/5+ % 25 sand mixture and % 2–4 bentonite) was carried out under 3 bar pressure to reduce the density of the concrete fill and recover the strength of the weakened zone around this section. A total of 44.2 t of cement was used during this process. A total of 12 drainage pipes (length: 6 m,/: 3 in.) were installed on both sidewalls to decrease water pressure behind the grouted zone. In addition to all these, a pattern (1.5–1.25 m) of rock bolts (length: 6 m, /: 28 mm) was applied between Ch:36 + 625 and 36 + 617 to limit deformation due to stress re-distribution during the advance of the tunnel face. Thus, the propagation of collapse was stopped and safety conditions required to resume the excavation were established (Fig. 6).

210. 瓦解区(CH:36617六百一十损害C36) 发生倒塌的背后不敷区面临断层图像,急剧下降到 隧道. 出现大范围的倒塌,造成区内找到失败 断层及延迟装置必要的辅助人员在上一轮周期进行(CH间:36+625和36+617). 没有支持系统的初步bolting岩石,岩石非常强调集体性的放松和削弱或粘质的物质 发生故障导致图像collapse.initially,流经水开始左sidewall 首项所规定的天然液压梯度,并逐步扩大为侵蚀区地上. 终于,隧道92M3充满碎片崩溃(附图6). 流动比率达到3记录这段L/S. 为防止疾病的崩溃,这一堆垃圾的其余部分支持面对迅速挖掘和实现稳定的外部材料. 这次共有28M3的喷射混凝土用于制造领域的倒塌20层Cmthick僵硬. 随后,又稳定措施,支持安装在CH:36+617和36+610人进行的顺序如下:(一)共33forepoling管(长度:6M/:1.5.)驱动沿屋顶部分倒塌面形成牢固冠; 铁丝网(乙)(/: C131损害131),在安装初期借助t喷浆层形车的螺栓; (C)增设16层,现厚喷浆(22M3)成立; (D)共有12个岩Bolts(长度:8M/:28毫米,最终负载:25T),27钢铁排骨先安装. 防止崩溃后区扩大,M344(20头)、80M3的具体喷射混凝土用于隧道恢复部分地区的崩溃. 然后用合并浇注 各种水泥混合比例(水泥/水的比例:1/17/5和7/5+25%砂和混合成2C4损害膨润土)进行三巴压力降低密度的水泥填补,恢复实力薄弱区周围这一节. 共计44.2t水泥用在这一进程. 共有12个排水管(长度:6M/:3.)设置在水压降低sidewalls背后压浆区. 除了这些,格局(150c1.25损害M)摇滚Bolts(长度:6M/:28晚上)之间适用CH:36+625和36+617限制变形因压力重新分布在预先隧道面. 因此,宣传安全生产条件和必要的崩溃停止继续挖掘成立(附图6).